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#1
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![]() rk wrote: I recall reading somewhere about a GPC fault on the first ALT flight. But I'm not sure and was chatting about this with a friend. A search turned up nothing, perhaps we are old and have bad memories? Or the correct report is sitting nearby hiding in plain sight? -- rk, Just an OldEngineer "The number of people having any connection with the project must be restricted in an almost vicious manner. Use a small number of good people." -- Kelly Johnson, as quoted in _Skunk Works_ Space shuttle orbiter approach and landing test evaluation report. Captive-active flight test summary - Sep 1, 1977 http://ntrs.nasa.gov/archive/nasa/ca...1978002256.pdf Shuttle ALT Captive-Active Flight 1A - June 17, 1977. General Purpose Computer 3 failed during preflight checks. Section 6.6, Page 6-10 (PDF page 71). Rusty |
#2
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![]() Rusty wrote: Space shuttle orbiter approach and landing test evaluation report. Captive-active flight test summary - Sep 1, 1977 http://ntrs.nasa.gov/archive/nasa/ca...1978002256.pdf Shuttle ALT Captive-Active Flight 1A - June 17, 1977. General Purpose Computer 3 failed during preflight checks. Section 6.6, Page 6-10 (PDF page 71). There's no real point in even voting on who's the most valuable SSH contributor of the year any more, is there? :-) Pat |
#3
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rk wrote:
Oh, and whilst I have the hood up, for STS-9, I think I heard this during a talk, again, the time of year to chase down these little items, wasn't there two GPCs that had trouble? Particles in the IC packages' cavities? Again, from memory, but trying to track these things down. I started a presentation on avionics redundancy about a year ago and picking it up again now. So your help is appreciated. STS-9 SSVEO IFA List GPC 1 failure caused by metal-particle-induced short circuit - Page 16 http://www.jsc.nasa.gov/news/columbia/anomaly/STS9.pdf STS-9 MISSION REPORT http://members.aol.com/WSNTWOYOU/STS9MR.HTM http://members.aol.com/WSNTWOYOU/mainmr.htm "GPC-1 And GPC-2 Failed - At 342:11:10:21 G.m.t., during computer reconfiguration for entry, GPC-1, (OPS 2) failed. Shortly thereafter at 342:11:16:45 G.m.t., GPC-2 (OPS 2) also failed. All attempts to bring GPC-1 back on line were unsuccessful. A ground review of GPC-2 memory dump indicated some memory alterations had occurred. However, GPC-2 was reinitialized in OPS 3 and was used in the redundant set with GPC-3 and GPC-4 for entry and landing. At Orbiter nose wheel touchdown (342:11:16:45 G.m.t.) GPC-2 again failed." Rusty |
#4
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![]() rk wrote: Wow. Mucho thanks. And there got to be an award here someplace. OM, can use some help here. Perhaps a rusty trinket awarded to whomever responds with the appropriate .pdf before rusty? -- rk Wait, there's more. Space Shuttle In-Flight Anomaly Database for STS-1 Through STS-107 http://www.jsc.nasa.gov/news/columbia/anomaly/ STS-66 / FLIGHT 66 MISSION REPORT GPC4 MMU-1 interface problem - page 9 http://www.jsc.nasa.gov/news/columbia/anomaly/STS66.pdf http://members.aol.com/WSNTWOYOU/STS66MR.HTM During a systems management (SM) checkpoint from general purpose computer (GPC) 4 to mass memory unit (MMU) 1 at 315:13:26 G.m.t. (07:20:26 MET), two error messages (I/O ERROR MMU 1 and S60 CHECKPT FAIL) were annunciated. The checkpoint was unsuccessful. During troubleshooting, all further transactions between GPC 4 and MMU 1 failed. Successful transactions were performed between GPC 1 and MMU 1. This interface problem between GPC 4 and MMU 1 was believed to be due to a failure of the GPC 4 bus control element (BCE) 18 transmitter and/or receiver. A software dump of GPC 4 was performed, and analysis of the dumped data supported the BCE 18 failure and indicated no other problem with GPC 4. A verification of GPC 4 as a redundant guidance, navigation and control GPC was performed at 316:18:30 G.m.t. (09:01:30 MET). The SM function was moved from GPC 4 to GPC 3. GPC 4 was then placed in the redundant set with GPC 1 at 316:19:13 G.m.t. (09:02:13 MET) to determine whether the problem that the GPC 4 interface had with MMU 1 also affected GPC 4 communications on the flight critical (FC) 8 data bus. The test confirmed that GPC 4 communications on FC8 were nominal, isolating the problem to the GPC 4 BCE 18 interface with MMU 1. The condition did not impact entry procedures. STS-51 / FLIGHT 57 MISSION REPORT http://members.aol.com/WSNTWOYOU/STS57MR.HTM The crew completed all stowage requirements and prepared the vehicle for entry and landing. The payload bay doors were closed and general purpose computers (GPCs) 1 and 2 were transitioned to OPS 3. However, during the redundant set expansion to include GPCs 3 and 4, GPC 3 failed to sync at 264:06:17 G.m.t. (08:18:32 MET). An initial program load (IPL) of GPC 3 was accomplished and the GPC was successfully brought into the redundant set. This GPC 3 failure-to-sync was initially thought to be explained by Operations (OPS) Note 42433; however, subsequent analysis removed this condition as a possible explanation. No explanation is currently known. STS-32 Backup Flight System GPC errors - Page 15 http://www.jsc.nasa.gov/news/columbia/anomaly/STS32.pdf Deorbit delayed 24h due to fog at landing site, then postponed to the next orbit because of a computer (GPC#5) failure. STS-41D Launch on Jun 25 postponed by 24h due to a GPC fault. GPC-5 failed - Page 2 http://www.jsc.nasa.gov/news/columbi...aly/STS41D.pdf Rusty |
#5
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I recollect in a simulation shortly before STS-1, the
entire redundant set crashed. I think it was an abort sim. Does anybody remember the details of that? -- Joe D. |
#6
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![]() "Joe D." wrote in message .. . I recollect in a simulation shortly before STS-1, the entire redundant set crashed. I think it was an abort sim. Does anybody remember the details of that? You may be thinking of the first launch attempt where the computers didn't synch up and they had to abort. -- Joe D. |
#7
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"Greg D. Moore (Strider)" wrote in message
nk.net... "Joe D." wrote in message .. . I recollect in a simulation shortly before STS-1, the entire redundant set crashed. I think it was an abort sim. Does anybody remember the details of that? You may be thinking of the first launch attempt where the computers didn't synch up and they had to abort. No there was a sim not long before STS-1 (which used essentially the GPC PASS flight software) where they were doing an abort and it exposed a software problem that crashed the entire redundant quad -- a big X on every screen. I recall some comment about John Young being upset, since the software was supposedly flight ready and they weren't that far from launch. I can't remember if the simulator had the fifth GPC with BFS (Backup Flight Software) running or not. I can't find any info on it, but I'm positive I remember that. -- Joe D. |
#8
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![]() Joe D. wrote: I recall some comment about John Young being upset, since the software was supposedly flight ready and they weren't that far from launch. If that would have been me, there would have been a big yellow puddle on the floor and a resignation letter on someone's desk inside of five minutes. Pat |
#9
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On Fri, 30 Dec 2005 16:59:36 GMT, "Greg D. Moore \(Strider\)"
wrote: "Joe D." wrote in message . .. I recollect in a simulation shortly before STS-1, the entire redundant set crashed. I think it was an abort sim. Does anybody remember the details of that? You may be thinking of the first launch attempt where the computers didn't synch up and they had to abort. It was just before STS-2. See: " The Space Shuttle Primary Computer System," Communications of the ACM, September 1984 Volume 27 Number 9, p. 886. http://klabs.org/DEI/Processor/shutt...ter_system.pdf |
#10
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"rk" wrote in message
... It was just before STS-2. See: " The Space Shuttle Primary Computer System," Communications of the ACM, September 1984 Volume 27 Number 9, p. 886. http://klabs.org/DEI/Processor/shutt...ter_system.pdf Rk, thanks for the info. It turns out John Young wasn't involved. Summary (as told by Jack Clemons, manager of avionics flight software at IBM): STS-2 delayed at last minute due to fuel spill damaging tiles, so crew (Engle & Truly) returned to Houston for more simulation. They were doing a TAL abort, and upon OMS fuel dump all four GPCs locked up, indicated on the cockpit displays as a big 'X" on each screen. Clemons said "the crew was rather upset, and they went off to lunch." Cause was an error in a software routine used for OMS fuel dump (essentially firing the OMS engines). In the abort sim, two OMS dumps were done, and after the first, counters in the software routine were not properly reset. The second time an uninitialized counter was used to calculate a GOTO which resulted in jumping into non-executable code (I assume data), resulting in a CPU spin. -- Joe D. |
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